… but Loy Yang A1 trips on Sunday 14th January 2024
A quick PS to the earlier Sunday article (which looked at LYA4) this time focused on LYA1.
A quick PS to the earlier Sunday article (which looked at LYA4) this time focused on LYA1.
Following the 4th successive trip/outage at Loy Yang A4 in recent days - and updating Tuesday's earlier article.
A quick look at 3 successive trips at Loy Yang A4 in returning back from a recent forced outage.
Yesterday (Tue 26th Sept 2023) we saw Kogan Creek drop offline for a few hours - and were asked if this was related to industrial action. Here, with the benefit of 'next day public'...
It does not happen often, so when receiving 4 different 'coal unit off' alerts within 24 hours, we thought we would take a look ...
CS Energy's Kogan Creek restarted on the morning of Tuesday 20th December 2022.
Prompted by a few media questions (on a day when all 4 units were offline together for about 3 hours), have taken a quick look at the status of the four units on the...
Alerted via an ABC news article, we take a quick look at Callide C3.
A short article, noting trip of Gladstone units 3 and 4 this afternoon.
Adding into the tight supply-demand dynamic, the coal-fired unit Tarong unit 2 tripped this afternoon.
A pretty rare event in the NEM, when two units trip simultaneously ... so a short article on WattClarity as a result.
The publication by AGL Energy of the short note about the transformer incident (and injured worker) at Liddell unit 3 yesterday prompted me to have a quick look, following on from the volatility this...
Earlier this afternoon we were alerted to a price spike in NSW and QLD that was seemingly caused by a unit trip at one of the larger generators in NSW.
Alerted to a price spike at 09:45 this morning in the QLD region, we discovered some reduction in load (spot-exposed Demand Response probably) and also a large collective trip in Solar Farm output (reasons...
Third case study today - and last one looking back at 2013. This one is a bit more complex than the first two.
Like was the case on 4th July 2013, the cause of this large Aggregate Raw Off-Target result (across all Semi-Scheduled Generators) was a single unit trip.
Does not take long to see why this particular dispatch interval was one of the few dispatch intervals (before 2019!) flagged in our top-down analysis of aggregate Raw Off-Target across all Semi-Scheduled units in...
Following on from Tuesday's main article (summarising results across 105,120 dispatch intervals through 2019 for 'all Coal' and 'all Wind' groupings), this is the first of 4 x Case Studies that look at each...
A quick look at Saturday 11th April (Easter Saturday) where there were major reductions in output at 4 units across Victoria - 3 coal units in the Latrobe Valley and the Macarthur Wind Farm...
Guest author, Allan O'Neil does a masterful job with limited time in reviewing some of the goings-on in the NEM (particularly VIC and SA) on Thursday 30th January 2020