Four coal unit outages in the past 24 hours
It does not happen often, so when receiving 4 different ‘coal unit off’ alerts within 24 hours, we thought we would take a look …
It does not happen often, so when receiving 4 different ‘coal unit off’ alerts within 24 hours, we thought we would take a look …
CS Energy’s Kogan Creek restarted on the morning of Tuesday 20th December 2022.
Prompted by a few media questions (on a day when all 4 units were offline together for about 3 hours), have taken a quick look at the status of the four units on the Callide Power Station site.
Alerted via an ABC news article, we take a quick look at Callide C3.
A short article, noting trip of Gladstone units 3 and 4 this afternoon.
Adding into the tight supply-demand dynamic, the coal-fired unit Tarong unit 2 tripped this afternoon.
A pretty rare event in the NEM, when two units trip simultaneously … so a short article on WattClarity as a result.
The publication by AGL Energy of the short note about the transformer incident (and injured worker) at Liddell unit 3 yesterday prompted me to have a quick look, following on from the volatility this week.
Earlier this afternoon we were alerted to a price spike in NSW and QLD that was seemingly caused by a unit trip at one of the larger generators in NSW.
Alerted to a price spike at 09:45 this morning in the QLD region, we discovered some reduction in load (spot-exposed Demand Response probably) and also a large collective trip in Solar Farm output (reasons unclear).
Third case study today – and last one looking back at 2013. This one is a bit more complex than the first two.
Like was the case on 4th July 2013, the cause of this large Aggregate Raw Off-Target result (across all Semi-Scheduled Generators) was a single unit trip.
Does not take long to see why this particular dispatch interval was one of the few dispatch intervals (before 2019!) flagged in our top-down analysis of aggregate Raw Off-Target across all Semi-Scheduled units in the NEM….
Following on from Tuesday’s main article (summarising results across 105,120 dispatch intervals through 2019 for ‘all Coal’ and ‘all Wind’ groupings), this is the first of 4 x Case Studies that look at each of the extremes in outcome. This one is the dispatch interval featuring the greatest over-performance, collectively, across all coal units through 2019.
A quick look at Saturday 11th April (Easter Saturday) where there were major reductions in output at 4 units across Victoria – 3 coal units in the Latrobe Valley and the Macarthur Wind Farm out in western Victoria, probably related.
Guest author, Allan O’Neil does a masterful job with limited time in reviewing some of the goings-on in the NEM (particularly VIC and SA) on Thursday 30th January 2020
A brief overview of a stressful afternoon/evening in the NEM, where a confluence of events (heatwave-driven high demand, low wind, coal unit trip, etc…) drive LOR2 low reserve condition notice in both VIC and SA, and gear AEMO up to call on Reserve Trader (yet again!)
A quick look after the unit trip (including reported explosion) at Mortlake Unit 2
Following the notice from AGL Energy on Friday last week about the extended outage occurring at Loy Yang A unit 2, here’s some initial thoughts via WattClarity (with more to come as time permits)
The framework we used to analyse the extent to which coal-fired power is “dependable” in the Generator Report Card, and the extent to which it’s been changing.