As noted in the snapshot from ez2view above, the unit tripped from 308MW in the 15:40 dispatch interval (NEM time), and that this outage was not previously notified in the ‘Generator Outages’ widget in ez2view.
Paul was one of the founders of Global-Roam in February 2000. He is currently the CEO of the company and the principal author of WattClarity. Writing for WattClarity has become a natural extension of his work in understanding the electricity market, enabling him to lead the team in developing better software for clients.
Before co-founding the company, Paul worked as a Mechanical Engineer for the Queensland Electricity Commission in the early 1990s. He also gained international experience in Japan, the United States, Canada, the UK, and Argentina as part of his ES Cornwall Memorial Scholarship.
Following on from Tuesday’s main article (summarising results across 105,120 dispatch intervals through 2019 for ‘all Coal’ and ‘all Wind’ groupings), this is the first of 4 x Case Studies that look at each of the extremes in outcome. This one is the dispatch interval featuring the greatest over-performance, collectively, across all coal units through 2019.
Tristan Edis of Green Energy Markets discusses the practicalities of the gap that must be filled by the gas sector under the nuclear power timeline proposed by the Federal Opposition.
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