One of the alerts triggered by ez2view overnight was with reference to the content in Market Notice 117908 from the AEMO, published at 01:02:
——————————————————————-
MARKET NOTICE
——————————————————————-
From : AEMO
To : NEMITWEB1
Creation Date : 28/08/2024 01:02:22
——————————————————————-
Notice ID : 117908
Notice Type ID : POWER SYSTEM EVENTS
Notice Type Description : Emergency events/conditions
Issue Date : 28/08/2024
External Reference : Non-credible contingency event – VIC region – 28/08/2024
——————————————————————-
Reason :
AEMO ELECTRICITY MARKET NOTICE.
Non-credible contingency event – VIC region – 28/08/2024
At 0001 hrs the APD No1 Potline and the APD No 2 Potline tripped.
AEMO did not instruct load shedding.
The cause of this non credible contingency event is not known at this stage.
Manager NEM Real Time Operations
——————————————————————-
END OF REPORT
——————————————————————-
Out of curiosity, this morning I’ve had a look at our trace of mainland frequency to see what happened at the time of the trip:
We can see a jump in frequency that lines up … but still within the bounds of the NOFB.
Referring back to NEMwatch with this snapshot at 08:00 this morning, we can clearly see the drop in ‘Market Demand’ reflected just after* AEMO became aware of the trip.
* remembering that ‘Market Demand’ is a forward looking measure for demand at the end of the dispatch interval used as an input into NEMDE in the dispatch process.
There’s also an earlier jump in demand at ~23:00 NEM time on Tuesday 27th August 2024 that has not been investigated.
Finally, the potlines returned to service, as the AEMO noted in Market Notice 117908:
‘——————————————————————-
MARKET NOTICE
——————————————————————-
From : AEMO
To : NEMITWEB1
Creation Date : 28/08/2024 02:17:12
——————————————————————-
Notice ID : 117909
Notice Type ID : POWER SYSTEM EVENTS
Notice Type Description : Emergency events/conditions
Issue Date : 28/08/2024
External Reference : Update – Non-credible contingency event – VIC region – 28/08/2024
——————————————————————-
Reason :
AEMO ELECTRICITY MARKET NOTICE.
Update – Non-credible contingency event – VIC region – 28/08/2024
Refer AEMO Electricity Market Notice 117908
At 0134 hrs the APD No 2 Potline was returned to service.
At 0200 hrs the APD No 1 Potline was returned to service.
The cause of this non-credible contingency event has been identified and AEMO is satisfied that another occurrence of this event is unlikely under the current circumstances.
AEMO will not reclassify this event as a credible contingency event.
Manager NEM Real Time Operations
——————————————————————-
END OF REPORT
——————————————————————-’
Nothing further, at this point.
Be the first to comment on "Jump in mainland System Frequency, coincident with potline trip at Portland smelter"